I installed a 280 jet.
now it runs, but it bogs, if I turn mixture screw out a half a turn from closed position, it idles good, if I turn out to 1 and 1/2 it bogs and wont idle, thats w/ rear air tube removed from carb, did this when adjusting cable, kept eye on piston so I wasn't using the cable for an idle adjustment.
Going to go to a 270 jet, figure im right there,
no air leaks present, used carb clean and the WD40 method, no change in idle at all.
You have to do your adjusting with the air tube and airfilter in place.