Right, finally some proper progress guys.
It’s been an interesting last few weeks, with much thought being given to how this linkage business is going to work out. After getting my head around some leverage ratio physics, cutting, grinding, welding and measuring, I finally have something that is going to work.
Once we had the swingarm plugged together A-la-Lego style, we tacked it together and positioned the front bearing tubes with the swinger on the bike and zapped it all in place. That was the easy part.
Now for the linkage system…well goodness me I though the front end YFZ swap was complicated, this one had me stumped for a while. However at the end of the day, it is actually pretty simple. The bamboozling bit is that there are so many moving parts. I tried to build a 3D model to simulate the linkage, and although it helped get to grips with what was going on and what each component did and how it influenced the system, it never accurately showed me how it would work in real life.
My model looked something like this:
The trick turned out to be the relationship between ride height, the maximum and minimum travel measurements as well as the shock travel and linkage travel. All of these components need to work in harmony to have a rideable bike. You don’t want the shock to bottom out while your ride height is still far from compressed and vice versa.
Essentially what I did was get the seat height of my brothers YFZ450 and use that as a guide, being that that bike is well setup and suits me well, I thought using this would be a good benchmark. I then winched the frame, leaving the wheels behind to set the bike at the same seat height. We then fiddled with the shock and linkage to work out where it should sit. Once we found rough positions, it seemed as though the system would hang far too low below the bike, increasing the risk of damage from passing over rocks etc. To fix this we relocated the top shock mount by 30mm. We also relocated the bottom hole in the shock by 20mm. This made things a lot better and tucked the linkage away nicely under the swingarm.
The next step was to figure out what my linkage ratio is and what it should be. But wait, what is that? I hear you ask…The linkage ratio is the ratio of force applied along a lever. If you apply 1F to the axle, and your shock is located half way along the swingarm, your shock is exposed to 2F. This can be viewed as a ratio of 2:1. The bigger the ratio, the softer the system, a 1:1 ratio is very hard! Now on a bike such as the blaster with a fixed bottom shock position, this ratio is a constant. The advantage of a linkage is that it makes the suspension “progressive” This means that it actually changes the leverage ratio as it moves through the bikes travel. This means that the suspension is soft on the small bumps and firm on the big bumps!
Having the linkage positions clamped down, we could test a variety of different arrangements to give us what we need. We started by getting the ratio off of the 450. This is pretty simple! Set the bike at max extension without the spring. I suspended the chassis from a block & Tackle and then placed a jack under the axle carrier. I found a position on the axle and the frame and jacked the wheels up at 10mm increments. At each increment, I measure the shock travel. You then divide the wheel travel by the shock travel and that gives you a linkage ratio!
I used some angles obtained via an inclinometer app on my phone to position the blaster linkage as closely as possible to the 450’s and then tested my linkage ratio. As you can see, my first two attempt gave a much more aggressive ratio, meaning the bike would be softer at first and then harder at the end of the travel. At least it was doing the right thing and the graph was showing it was a progressive system and not regressive!
After we did the shock shortening and a few other things I retested and found something remarkable. My linkage ratio came out near exactly the same as the 450!
Happy with that, we moved on the attachment and welding…
We came across a snag when welding up the front bearing tubes…once welded up, they turned oval ever so slightly. Just enough to prevent to bearing from being pressed in easily and when they were pressed in, they were deformed and wouldn’t allow the inner tubes to be inserted…We managed to solve this problem (temporarily) by sanding the holes, I still need to take it in to get machined to fix this properly!
After that, it was welding and welding. The tricky part being attaching the dog bone mounting to the frame. The blaster frame isn’t too thick and mine isn’t in the best condition along that back frame bar.
Finally I was relieved to find that my shock cut-out on the swingarm was just big enough and that the spring passed though and operated well within the cut-out I had made.
Now I have the bike standing and it feels good. Wheel travel is 2mm more than the YFZ450. Not bad I think!
I have to still resolve my bearing issue and finish off a few welds.