Today I discovered as i were messing with my blaster it were running like crap like when ever i let off the gas or the choke pop in it would bog out... and as a result i checked my carb and it had a #280 Main Jet from my new carb rebuild kit and my old one were actually a #360 main jet... Should my blaster with these mods have a #360... And for any one else use this as a tip to why your blaster may be bogging out even though it runs. Change your Main jet by ordering a Main Jet Kit... And Could that possibly blow my motor...
Well I have:
.010 Wiseco Piston n Bore
Boysen Reeds
Uni Air Filter w/ No lid
Oil Injection Delete w/ 32:1 Mix Ratio
Well I have:
.010 Wiseco Piston n Bore
Boysen Reeds
Uni Air Filter w/ No lid
Oil Injection Delete w/ 32:1 Mix Ratio