so i put a mikuni 28mm flatside carb on the 04 with a 260 main jet like it had with the old carb but now its running super rich. tried every jet between 260 and 320 and it always seemed super rich. went down to a 240 and it was still really rich but would atleast move. took the air box lid off just to see if it would help and it livened right up but idle is unpredictable and has a killer bog as soon as you hit the throttle, its hard to start, and you can hear the reeds flutter weird and loud when you touch the throttle but it goes away when you ride. i want to put the lid back on and get it tuned up but im having trouble wraping my head around why it would need a 220-230 main jet, with the mods i'd expect it to need 260-280.
carb settings.
pilot unsure bought carb used
needle second notch from the top
main 240
idle screw 2 and a half out
fuel/air screw 11/2 out
mods
k&n style filter
boysen pro series 2 stage reeds
vitos reed spacer
pro circut pipe
mikuni 28mm flat side carb
lid is off but i want it on.
with that said why would it need a stock or smaller than stock main to run right?
seems my machines spend more time not running than they do running. all the problems are driving me nuts these days especially since trying to get the old red and black beast running and finding out i have no spark and that i need to re split the bottom end because i have no neutral after sending it out to have a 3mm stroker crank installed and 4deg key.
carb settings.
pilot unsure bought carb used
needle second notch from the top
main 240
idle screw 2 and a half out
fuel/air screw 11/2 out
mods
k&n style filter
boysen pro series 2 stage reeds
vitos reed spacer
pro circut pipe
mikuni 28mm flat side carb
lid is off but i want it on.
with that said why would it need a stock or smaller than stock main to run right?
seems my machines spend more time not running than they do running. all the problems are driving me nuts these days especially since trying to get the old red and black beast running and finding out i have no spark and that i need to re split the bottom end because i have no neutral after sending it out to have a 3mm stroker crank installed and 4deg key.