i removed the tors from my daughters blaster because i thought it was sticking coming back down to idle and at the same time i replaced the pilot jet to a 35. my problem is it comes down to an idle in stages like it has an air leak. i did a leak down test it holds 10psi for half an hour the top end only has about 3hrs on it. i sprayed starting fluis all over all the mating surfaces that it could possably have an air leak byt nothing! did not rev at all!!! it has a toomey B1 pipe, boysen reeds, k&n pod filter, tors removed and a mild clean up port/polish. any help would be appriciated i have spent hours trying to get it right and am getting frustrated and just about ready to give up and reluctantly take it to the shop. i have heard that the toomey pipe can be tricky to tune around any comments about that??????????????????