blaster doesnt run right

Yes most certainly get a new plug. The gunk on top of your plug and on the coil was most likely dielectric grease. Previous owner probably put it there. If so than that's fine. When you get a plug grab a few if you can.
 
ok. the one I pulled off at first was thick and black and wet, and the one I had lying around was just thick and black.and its the br8es
 
Grab a few new plugs if you can but definetly throw a new plug in there. Get back to us after you put a new plug .

If she starts up and runs ok. Don't ride it for long. You got to up the jets leak test and plug chop.
 
Grab a few new plugs if you can but definetly throw a new plug in there. Get back to us after you put a new plug .

If she starts up and runs ok. Don't ride it for long. You got to up the jets leak test and plug chop.
 
ok. I adjusted the float height to 20mm. it was at about 23mm before. the main jet is a 230. and I checked the reeds a few days ago and I flipped them to be flush. and it still did the same thing. I thought it worked for a little bit but then same thing. the motor is stock other than someone lightly ported it. and I mean lightly. like I said fmf fatty and fmf silencer. airbox lid on. I still have the carb of. anything else I should look for? and I just cleaned it twice. took it all apart and sprayed with carb cleaner. didn't help.

#230 is no way big enough, the FMF Fatty calls for a #260, Air filter one size more and 32:1 one more again.

Start with a #290 main and plug chop.

Before you make the plug chop run it is important that the float level is correct, the idle is set correctly and there are no air leaks in the system, otherwise the smoke ring may lie about the AFR.

WHEN ALL OF THE ABOVE ARE CORRECT PROCEED WITH THE FOLLOWING.

Warm up motor to operating temp.

Fit new B8ES plug, ride WOT through the gears and hold WOT in 5th or 6th gear for 10 seconds, or as long as you can safely.

Switch off the motor and pull in the clutch, apply brakes to come to a stop quickly.

Take the plug out and replace the old one for the ride home.

Carefully cut the threaded end off the plug to expose the insulator.

There should be a smoke ring of a cardboard or biscuit colour around the insulator.

If it is non existant or a very light colour, you are lean and require a larger main jet.

If it is a lot darker you are rich and may go down a size in main.

I prefer to run a little on the darker side, I may loose a little power but it is worth it for the peace of mind that I won't need a rebuild so soon.

http://www.blasterforum.com/do-yourself-20/how-plug-chop-38674/

http://www.blasterforum.com/engine-13/plug-chop-how-vid-48226/

This is a good to go plug.

2wr2fwo.jpg



This one is a little rich, but I would run it, I like to be on the safe side.

plug152mainmediumoi2.jpg
 
Ok. So it started up but after a while still bogged and did the same thing just not as bad. And another thing, wen I started to bog if I shake the quad it revs rite up.
 
Yea I've checked that a few times. I've even drained the fuel through that gas line and it flowed nicely.

how much fuel did you drain? if the vent on the cap is clogged then it will drain nicely until the tank gets vacuum locked then it will stop flowing. try to fill at least a snapple bottle size bottle
 
Ok. So it started up but after a while still bogged and did the same thing just not as bad. And another thing, wen I started to bog if I shake the quad it revs rite up.

that sounds fuel or loose electrical connection to me.

you've already checked fuel flow to the carb, it could be the fuel sloshing around in the bowl, either picking up more or less
check/set float height......
http://www.blasterforum.com/carburetor-138/float-heights-how-adjust-them-50565/

check all electrical connections for loose/dirty
 
If it improves when you shake it there are a number of things that could be wrong.

Low fuel in tank, delivery tube above the level.

Float level set wrongly ,allowing fuel to flow when disturbed.

Sticking float.

Air leak made worse by movement, this happens sometimes around the carby boot.
 
Like Awk said. It sounds like it maybe electrical. Check your grounds and fit any cuts or bare wires..
 
ok. any specific connections tht mite cause this? and it shoots quick flames out of the exhaust. flywheel key??