So after I crashed my blaster two Sundays ago, I drove it back to the truck just fine, but I was taking it easy cause of the broken rib. When it got back to my sisters house, after a long cool down period, I started it right up n drove it across the street to my house n it sounded like it had a really bad knock in the motor. So I parked it, built a leak down tester n did a leak test. Besides a very small leak from the seal in the intake boot most likely due to the adapter I used. I found no other leaks anywhere so I put it back together and started it and took it for an easy ride(cause I'm still in pain). No air leak found n I still can't have the air screw out more then a quarter turn. Why would this be so?what could cause this? It is stock, air box lid gone n a 250 main jet with the stock idle jet n needle. I just want to make sure I don't do any damage.
Thanks in advance for all your help
Arnold
Thanks in advance for all your help
Arnold