30 pilot 340 main stock carb needle middle clip. Lrd pipe airbox outerwairs lid. Starts and idles perfectly does this weird surging at WOT. YouTube vid enclosed.
plug chops determined the 340 main ?
30 pilot ?
how many turns out on the airscrew gave you highest idle with the stock pilot that determined you needed to go leaner ?
https://www.blasterforum.com/threads/adjusting-your-airscrew-pilot-jet.51060/
I've tuned a bunch of blasters in all states of tune and various pipes, including an LRD, not one wanted anything besides the stock 32.5 pilot (high idle less than 2 turns out on airscrew)
unless your at some "in the clouds" elevation ?
leakdown tested ?
float height correct ?
fuel cap vent working ?
reeds good ?
don't count out an electrical situation, they like to show themselves under load and act just like a fuel problem.
TORS deleted ?
ground at coil to clean bare frame ?
unplug key and kill switch one at a time to count them out
unscrew plug cap, inspect up inside, if good cut 1/2" off wire and re-screw it back on
if burnt or jenky looking, replace with NGK screw on cap from auto store
Ok I'll try it I gotta find a runway to get it up there lolTry the plug chop again, wide open into 5th/6th gear ?
Ok I'll try it I gotta find a runway to get it up there lol
Sorry forgot to reply to your message so you get a notificationTry the plug chop again, wide open into 5th/6th gear ?
Well I'm dumb runs 100% better now. How do those look?