First off, if you haven't seen my posts before, I've had some odd issues with the way my Blaster runs and even with all the motor work I've had done, it can't beat a 400ex in a drag...just to give you an idea of the power. Now, I originally had my porting and head work done by Marc Cross at Hollywood Dirt. He did a great job and I requested my head be milled 0.030 off......I even mic'ed it and that's what it was when I got it back.
Anyways, through 1-3 gears it pulls well, but then slowly tapers off through 4-6....yes natural I know, but more so than normal. Jetting is fine. So I theorized that the 30mm carb was too small and it is in a lot of respects, but I wouldn't have thought THAT much so. So I purchased a 35mm carb to put on it and give it a whirl. Before switching over, I want to do a leakdown test and compression test to see where I'm at. I lost my old compression tester so I bought a new one and got it in the mail today. I just went out and did the compression test on my Blaster.......found out really great news.....I definitely don't need a rebuild.....but also found out some rather alarming news.....I'm running at 175psi while running 93 octane. :-/ If the head was milled to spec, how is this happening? Can I squeak by with 93?....I really didn't want to run higher octane race fuel as it's a biotch to come by. I thought maybe carbon deposits on the piston, so I took a flashlight to the piston through the plug hole.....not spic and span clean on the surface, but nothing out of norm and there are no significant carbon deposits. This sh*t is confusing. :-/
Anyways, through 1-3 gears it pulls well, but then slowly tapers off through 4-6....yes natural I know, but more so than normal. Jetting is fine. So I theorized that the 30mm carb was too small and it is in a lot of respects, but I wouldn't have thought THAT much so. So I purchased a 35mm carb to put on it and give it a whirl. Before switching over, I want to do a leakdown test and compression test to see where I'm at. I lost my old compression tester so I bought a new one and got it in the mail today. I just went out and did the compression test on my Blaster.......found out really great news.....I definitely don't need a rebuild.....but also found out some rather alarming news.....I'm running at 175psi while running 93 octane. :-/ If the head was milled to spec, how is this happening? Can I squeak by with 93?....I really didn't want to run higher octane race fuel as it's a biotch to come by. I thought maybe carbon deposits on the piston, so I took a flashlight to the piston through the plug hole.....not spic and span clean on the surface, but nothing out of norm and there are no significant carbon deposits. This sh*t is confusing. :-/