Sooo 3rd post here lol. Was going to get rid of this one because of the headaches but made a little progress that's worth trying to salvage it. So I have this blaster. Thought it was a 2000 turns out to be a 88 according to the VIN. Not 100% it is but pretty sure. Anyways. Bought it from the guy, didn't start at the time, took it home pull started it and ran. Always had to pull start it but it would run amazing when it started. Would keep up with my brothers Polaris 250. Had some bogging issues after a week so I figured it was a good time to clean the carb gas etc. Got my kit installed everything and put it back together, started but ran like crap. So I did some changes and it wouldn't fire at all. Sooo after a couple days I put the 250 main that was in it before back in it. Kinda ran but after awhile it'd die. And not start and didn't start for a day or two. So I started going back to the original settings that the previous owner had it at. #250 main, stock pilot jet. Needle clip in 2nd notch. Started to run a little but then would bog out and die like it was loading up. Messed with air screw and air fuel screw. Nothing changed. So I put the original mikuni needle back in (it was slightly bent at the bottom but at that point was trying anything) put the original pilot jet in and the 250 main they had in it. Started up fine no problems. But once it got warm it would bog and neither of the screws would help or worsen it. Kinda out of ideas and ready to sell it or take it to the shop. So close but I'd rather make money on this thing then shovel out more money on someone else fixing it. I know it can't be anything major because it starts up and runs fine till operating temp. I'd definitely appreciate the help. Hoping this thread gets a little more help then my last two
Also the mods on this as far as I know and can see are, air box lid off, tors removed but not off the carb, DG header, stock silencer, and presumably the stock filter. Everything else seems stock.
I'm really hoping to ride this thing more then I have. First four wheeler I've owned and already hooked but problems are getting the best of me
Also the mods on this as far as I know and can see are, air box lid off, tors removed but not off the carb, DG header, stock silencer, and presumably the stock filter. Everything else seems stock.
I'm really hoping to ride this thing more then I have. First four wheeler I've owned and already hooked but problems are getting the best of me