Okay let me give the full story so everyone knows what is going on. I know there are other threads out there about this issue but they have not been successful for me. I run my own small engine business and have done everything to this thing that I can think of and nothing changes. This is for a customer of mine and I would like to get him his bike back as soon a possible but I must be missing something. Any help would be greatly appreciated.
Symptoms: It came to me with no spark as the primary problem. Blaster will start almost first kick every time and will idle somewhat with what sounds like a miss, pop, or ping, sort of like something running out of time. If I give it gas it just bogs out and will not go up at all. If I let off of the throttle it will idle for a few seconds then die.
What I have tried: Bought a new stator off of Ebay (which has the adjustable timing slots), a new coil, and a carburetor kit.
I put the stator in as close to the same place I could tell as the old one and even tried the +4 option but no difference. Cleaned the petcock and the filters on it and the tank with fresh premix. I pulled the reeds and cage out and they seemed a little wet but that was before the carburetor was rebuilt and they were seating with no gaps and the rubber on the cage looked smooth. I flipped them over anyway just in case they weren't springy enough. I can't find any air leaks and I have bypassed the TORS system.
I then took the header and muffler off and made sure they were clean and flowing. I tried another new spark plug as well. I set the float height at 20MM and the main jet needle is at the third groove down. New main jet is a 230 and the new pilot jet is 32.5 which I believe is all stock. I even took out the main jet holder and cleaned it and made sure the 8 holes were clean and flowing. The compression checked out between 80-85 which seems low to me but I have a cheap guage and don't even know if it works correctly. I was told that the guy that bought this blaster was told that it was bored over but I haven't torn down the top end and measured the bore so I can't confirm that. So basically I have gone through everything that is in my mechanical ability several times and nothing ever changes.
The choke position makes no difference and neither does the mixture screw. There doesn't seem to be a standard mark in the case for the stator plate but I saw the Ricky stator instructions show the "0" mark at the bottom edge of the lip that sticks out of the case near the grommet slot for the wires. Could I just be out of time? Maybe I'm just missing some stupid little thing. IDK but it sure does have me baffled! Everything is stock on this machine except the pump has been blocked off and it is running premix around 32:1 ratio.
Any ideas? Thanks!:-/
Symptoms: It came to me with no spark as the primary problem. Blaster will start almost first kick every time and will idle somewhat with what sounds like a miss, pop, or ping, sort of like something running out of time. If I give it gas it just bogs out and will not go up at all. If I let off of the throttle it will idle for a few seconds then die.
What I have tried: Bought a new stator off of Ebay (which has the adjustable timing slots), a new coil, and a carburetor kit.
I put the stator in as close to the same place I could tell as the old one and even tried the +4 option but no difference. Cleaned the petcock and the filters on it and the tank with fresh premix. I pulled the reeds and cage out and they seemed a little wet but that was before the carburetor was rebuilt and they were seating with no gaps and the rubber on the cage looked smooth. I flipped them over anyway just in case they weren't springy enough. I can't find any air leaks and I have bypassed the TORS system.
I then took the header and muffler off and made sure they were clean and flowing. I tried another new spark plug as well. I set the float height at 20MM and the main jet needle is at the third groove down. New main jet is a 230 and the new pilot jet is 32.5 which I believe is all stock. I even took out the main jet holder and cleaned it and made sure the 8 holes were clean and flowing. The compression checked out between 80-85 which seems low to me but I have a cheap guage and don't even know if it works correctly. I was told that the guy that bought this blaster was told that it was bored over but I haven't torn down the top end and measured the bore so I can't confirm that. So basically I have gone through everything that is in my mechanical ability several times and nothing ever changes.
The choke position makes no difference and neither does the mixture screw. There doesn't seem to be a standard mark in the case for the stator plate but I saw the Ricky stator instructions show the "0" mark at the bottom edge of the lip that sticks out of the case near the grommet slot for the wires. Could I just be out of time? Maybe I'm just missing some stupid little thing. IDK but it sure does have me baffled! Everything is stock on this machine except the pump has been blocked off and it is running premix around 32:1 ratio.
Any ideas? Thanks!:-/